I never knew that such a measurement existed other than in cooking!
According to my "stupid" phone the Super VC10 had a capacity of 14,853,120 teaspoons of fuel precisely!
How long would that take to refuel I wonder!!
Imperial teaspoons!
- vololiberista
- Posts: 334
- Joined: Tue Jun 15, 2010 10:13 pm
- Location: LIMZ - CUF
-
- Webmaster
- Posts: 788
- Joined: Fri Aug 02, 2002 9:03 pm
- Location: Amsterdam
- Contact:
Imperial teaspoons!
I guess that depends. How many teaspoons can you use simultaneously?
- Tonkenna
- Posts: 684
- Joined: Sat Aug 10, 2002 7:32 pm
- Location: Boldly going!
- Contact:
Re: Imperial teaspoons!
About 172 days at 1 per second!
Please check out my Flickr account: http://www.flickr.com/photos/zz330/
-
- Posts: 22
- Joined: Tue Nov 13, 2007 8:42 am
- Location: Cambridgeshire
Re: Imperial teaspoons!
Would be a challenge for a QTR downroute, that is if you could get an imperial teaspoon!!!
- vololiberista
- Posts: 334
- Joined: Tue Jun 15, 2010 10:13 pm
- Location: LIMZ - CUF
Re: Imperial teaspoons!
I suppose stuck in a desert outpost somewhere, a call for a teaspoon from the galley to help refuel and a radio message saying the flight has been delayed 6 months for technical reasons!
-
- Posts: 29
- Joined: Wed Dec 10, 2008 2:21 pm
Re: Imperial teaspoons!
Following a smoke event during an air test, a rivet head was found in part of an air conditioning compressor. In order to rule out possible sabotage (this was around the time that 'Scrapheap Challenge' St.Athan was being handed over), a thorough search was conducted of the aeroplane, one of the RAF's ex-BOAC, ex-Gulf Air VC10K2s.
It was found that the 'stall dump' lever had probably never been connected as a vital pin was missing and the hole into which the pin was supposed to be fitted showed long term surface corrosion. The lift-rate modifier hadn't been connected either, as its cables were found to have been stuffed behind some insulation material.....
But most intriguingly, in the depths of the aeroplane a BOAC silver teaspoon was found! That must have been in the aircraft during its entire service time with Gulf Air, as well as conversion by BWoS into a K2.....and its subsequent career with the RAF.
The following air test went fine though and the aircraft was soon back at Brize.
It was found that the 'stall dump' lever had probably never been connected as a vital pin was missing and the hole into which the pin was supposed to be fitted showed long term surface corrosion. The lift-rate modifier hadn't been connected either, as its cables were found to have been stuffed behind some insulation material.....
But most intriguingly, in the depths of the aeroplane a BOAC silver teaspoon was found! That must have been in the aircraft during its entire service time with Gulf Air, as well as conversion by BWoS into a K2.....and its subsequent career with the RAF.
The following air test went fine though and the aircraft was soon back at Brize.